BH-CTRL ROOM
Tuesday, May 26, 2015
Sunday, April 26, 2015
Wednesday, April 22, 2015
17/04/2015
-
Unit
for loading up.
-
Unit
trip due hot reheat pressure measurement failure (turbine protection).
-
Unit
restart
At 11:10 turbine 3000 rpm ready to synchroniseClose to 12:00
Alstom advises that close to noon 17 April 2015, we experienced yet
another blackout event with consequent abnormal run-down of the Unit 6
turboset.
At the time of the event, the excitation unit (AVR) was on and the power train unit was about to be synchronised.
The details of the incident as currently understood and with a focus on impact on the turboset, follow - these will be corroborated by the Sequence of Events logger when such information becomes available.
At the time of the event, the excitation unit (AVR) was on and the power train unit was about to be synchronised.
The details of the incident as currently understood and with a focus on impact on the turboset, follow - these will be corroborated by the Sequence of Events logger when such information becomes available.
a. At about midday, an
electrical board tripped in-turn tripping the turbine. at this stage the
shaftline was running at 3,000 rpm with excitation on and synchronisation about
to start.
b. At
a shaftline speed of +800 rpm the main electrical board/main HV breaker
tripped resulting in a total blackout.
c. The
backup diesel generators failed to kick-in at this point and the shaftline
continued to run-down on emergency (DC) lube oil supply.
d. At +150
rpm the diesel generators kicked-in and as experienced with the blackout event
of 21 March '15, the controls/DCS showed the lube oil pump 'ON' but inspection
proved that it was actually 'OFF' and non-operational.
e.
Thus, shaftline had to be hand-barred on emergency lube oil, with jacking oil
running off the generators, for some time.
f. The
shaftline was eventually returned on to turning gear on emergency lube oil, and
jacking oil.
Status : 17/04/2015 at 18:15 :
-
Unit ready for turbine start (1 mill in
service – unit in by-pass operation)
-
Diesel generator 2 is working correctly
-
Diesel generator 3 is not working
correctly
-
ESKOM Engineering decided to stop the
unit and to re-commission the Diesel generators before next start-up
Thursday, April 16, 2015
16/04/2015
-
Boiler
Feed water flow tuning improved
-
11:03
Synchronisation and load up 356 MW. Boiler and feed water flow tuning.
-
14:10
Unit trip due to Boiler main steam temperature drop (Turbine protection):
Boiler load control problem.
-
18:00
Synchronisation: load steady (around 200 MW) over night.
Wednesday, April 15, 2015
15/04/2015
Between 13/04/2014 to
15/04/2014
-
Unit
6 restart on by-pass operation.
-
Feed
water flow tuning. This is the biggest interface problem (P02/P03/P17). PAC and
Belfort still struggling to find the right settings to tune this loop. Most of
the boiler trips are due to this function.
-
Boiler
economizer soot blowing (Hitachi). The boiler tube have never been cleaned
before: This may explain this difficulty to tune the boiler feed water flow.
Tuesday, April 14, 2015
Monday, April 13, 2015
Subscribe to:
Comments (Atom)