Tuesday, May 26, 2015

26/05/2015 - 1rst Full Load 803MW


1rst FULL LOAD ACHIEVED - 803MW

Sunday, April 26, 2015

Wednesday, April 22, 2015

17/04/2015



-          Unit for loading up.
-          Unit trip due hot reheat pressure measurement failure (turbine protection).
-          Unit restart
At 11:10 turbine 3000 rpm ready to synchronise

Close to 12:00
 Alstom advises that close to noon 17 April 2015, we experienced yet another blackout event with consequent abnormal run-down of the Unit 6 turboset.

At the time of the event, the excitation unit (AVR) was on and the power train unit was about to be synchronised.

The details of the incident as currently understood and with a focus on impact on the turboset, follow - these will be corroborated by the Sequence of Events logger when such information becomes available.

a. At about midday, an electrical board tripped in-turn tripping the turbine. at this stage the shaftline was running at 3,000 rpm with excitation on and synchronisation about to start.
b. At a shaftline speed of +800 rpm the main electrical board/main HV breaker tripped resulting in a total blackout.
c. The backup diesel generators failed to kick-in at this point and the shaftline continued to run-down on emergency (DC) lube oil supply.
d. At +150 rpm the diesel generators kicked-in and as experienced with the blackout event of 21 March '15, the controls/DCS showed the lube oil pump 'ON' but inspection proved that it was actually 'OFF' and non-operational.
e. Thus, shaftline had to be hand-barred on emergency lube oil, with jacking oil running off the generators, for some time.
f. The shaftline was eventually returned on to turning gear on emergency lube oil, and jacking oil.



Status : 17/04/2015 at 18:15 :
-          Unit ready for turbine start (1 mill in service – unit in by-pass operation)
-          Diesel generator 2 is working correctly  
-          Diesel generator 3 is not working correctly
-          ESKOM Engineering decided to stop the unit and to re-commission the Diesel generators before next start-up

Thursday, April 16, 2015

16/04/2015



-          Boiler Feed water flow tuning improved
-          11:03 Synchronisation and load up 356 MW. Boiler  and feed water flow tuning.
-          14:10 Unit trip due to Boiler main steam temperature drop (Turbine protection): Boiler load control problem.
-          18:00 Synchronisation: load steady (around 200 MW) over night.

Wednesday, April 15, 2015

15/04/2015




Between 13/04/2014 to 15/04/2014

-          Unit 6 restart on by-pass operation.
-          Feed water flow tuning. This is the biggest interface problem (P02/P03/P17). PAC and Belfort still struggling to find the right settings to tune this loop. Most of the boiler trips are due to this function.
-          Boiler economizer soot blowing (Hitachi). The boiler tube have never been cleaned before: This may explain this difficulty to tune the boiler feed water flow.

Tuesday, April 14, 2015

14/04/2015

Unit on By-Pass Operation

Monday, April 13, 2015

13/04/2015

Re-Start of Unit on By-Pass Operation