Saturday, March 14, 2015

14/03/2015

steady operation, no interruption:

-          Load between 200 & 350 MW.
-          Boiler tuning and mill testing.
-          Turbine in operation (load control).

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Friday, March 13, 2015

13/03/2015

FORECAST PROGRAMME




ACTUAL @7:30
-          Unit was running @ 120 – 150MW during the night
Program for today : Boiler tuning with one and 2 mills (Hitachi)


ACTUAL @23:00
-          8:27 Turbine on protection HP Exhaust High due to boiler load reduction
-          9:12 Synchronization
-          9:18 Turbine on protection HP Exhaust High due to boiler load reduction
-          Boiler shut down to restart with 2 draft groups, second mill cannot be started with only one draft group
-          16:30 Boiler fire in
-          19:00 Synchronization
-          20:32 Load 300MW
-          22:11 Boiler air heater motor high current, load reduced to 150MW
-          22:14 Turbine on protection HP Exhaust High due to boiler load reduction
-          22:30 Boiler shut down
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Thursday, March 12, 2015

12/03/2015

FORECAST PROGRAMME


ACTUAL @7:00
11/03/2015@22:52 Turbine trip due to high exhaust temperature HP
-          GCB didn’t open, and we get low reverse power (reverse power was not detected by gen protection device)
-          The case is under investigation


ACTUAL @18:00
-          Reverse power issue resolved by setting changes in the gen. protection relay
-          17:00 Synchronization
-          Reverse power test successful
-          17:20 Synchronization
-          Power increase to 150MW

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Wednesday, March 11, 2015

11/03/2015

FORECAST PROGRAMME



ACTUAL:

Status 11/03/2015 5:30

-          Hitachi PTW for crack repair closed @ 5:00
-          Boiler filling ongoing
-          Turbine start expected @ 14:00
-          Synchronization expected @ 14:15

ACTUAL@ 24:00
-          Unit was synchronized @ 16:52
-          18:06 Turbine trip due to LP heater 1 level transmitter problem
-          18:15 Synchronization and load increase up to 300MW with 2 mills in service
-          22:00 One  mill trip, load reduced to 180MW
-          Draft group trip due to gas air heater
-          Second mill trip
-          22:52 Turbine trip due to high exhaust temperature HP
-          GCB didn’t open, and we get low reverse power (reverse power was not detected by gen protection device)
-          The case is under investigation

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